SO SAD: Crystal palace three key players die in a plane crash….

The Munich air tragedy happened on February 6, 1958, when British European Airways Flight 609 crashed during

its third attempt to take off at Munich-Riem Airport in Munich, West Germany. The airplane was transporting the

Manchester United football squad, also known as the “Busby Babes,” as well as spectators and journalists.[1] There

were 44 individuals on board, and 20 of them died at the spot. The injured, some unconscious, were brought to

Munich’s Rechts der Isar Hospital, where three more died, for a total of 23 dead and 21 survivors.

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The Manchester United team was returning from a European Cup encounter in Belgrade, Yugoslavia (now Serbia),

where they defeated Red Star Belgrade to reach to the competition’s semi-finals. The flight made a stop in Munich to

refuel since the “Elizabethan”-class Airspeed Ambassador couldn’t fly nonstop from Belgrade to Manchester. After

refueling, pilots James Thain and Kenneth Rayment twice aborted takeoff due to boost surge in the left engine. Thain

vetoed an overnight stopover in Munich in favour of a third takeoff attempt, fearing they would fall too far behind

schedule.

Man United fans' celebrate FA Cup victory whilst Crystal Palace supporters  in despair | Daily Mail Online

By then, snow had fallen, forming a layer of slush at the runway’s end. After hitting the slush, the plane crashed

through a fence beyond the end of the runway, and the left wing was severed when it collided with a home. The tail

part detached and collided with a barn containing a parked gasoline truck, causing it to catch fire and explode. Thain

began evacuating passengers, fearing that the plane would also explode, while goalkeeper Harry Gregg assisted in the

recovery of survivors from the wreckage.

West German airport authorities initially blamed Thain, claiming he did not de-ice the aircraft’s wings, despite

eyewitness testimony indicating that de-icing was unnecessary.[2] The last inquiry by the United Kingdom Board of

Trade, published in 1969, determined that the crash was caused by snow slush on the runway, which delayed the

plane too much to allow takeoff, and that Captain Thain was not to fault.[3]

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